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TO STUDY THE POSSIBLE CAUSES AND TO ADDRESS THE HIGH PRESSURE DROP ISSUE ACROSS THE HTS CONVERTER CATALYST BED DUE TO COKE FORMATION

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dc.contributor.author Aleena Ahmed, Ahsan Munir, Huzaifa Bin Arshad
dc.date.accessioned 2022-09-14T04:56:13Z
dc.date.available 2022-09-14T04:56:13Z
dc.date.issued 2022-06
dc.identifier.uri http://10.250.8.41:8080/xmlui/handle/123456789/30456
dc.description Advisor: Dr. Tayyaba Noor
dc.description.abstract For Diesel hydro-desulfurization (DHDS), Attock Refinery Limited (ARL) uses hydrogen produced by the Hydrogen Production Unit. High Temperature Shift (HTS) Converter is an important part of this unit in which heterogeneous catalytic Water-Gas Shift reaction takes place. A high pressure drop across the HTS catalyst bed was reported. This project aims to study and address the possible causes of this pressure drop. For this purpose, the design of monolithic HTS Converter was proposed instead of the packed bed reactor. The proposed design simulated through COMSOL Multiphysics gave significant reduction in pressure drop. Moreover, to enhance the catalyst performance by reducing coke formation, this work further focused on optimization of various operational parameters. This in turn, reduced the plant downtime. Aspen HYSYS was used for simulation of complete hydrogen production unit. Economic analysis and HAZOP study was also carried out. en_US
dc.publisher SCME NUST en_US
dc.subject STUDY, POSSIBLE CAUSES, HIGH PRESSURE, DROP, ISSUE, ACROSS, HTS, CONVERTER, CATALYST, COKE FORMATION en_US
dc.title TO STUDY THE POSSIBLE CAUSES AND TO ADDRESS THE HIGH PRESSURE DROP ISSUE ACROSS THE HTS CONVERTER CATALYST BED DUE TO COKE FORMATION en_US
dc.type Thesis en_US


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